whippleofd
Posts: 617
Joined: 12/23/2005 Status: offline
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quote:
ORIGINAL: 1275psi 10/2/44 But enough of that, are you ready for your Ticket on the Turbo generator? Achieve this my young stoker, and its no more boiler room for you ney!, you can come over to the luxury of the engine room, where temperatures are so much lower, and the space so less claustrophobic. Ok then, away you go, I will be watching carefully........... You've done it a dozen times, ........... First, align the circulation pumps...and start them. Good Vent the condensor............bloody cock is so hard to reach Alright.........the condensor shows only a little in the glas, better back fill it....... Thats better. Hope its enough. Start the condensate pump on recirc, three turns should do it. Crud, better check it actually started............(some times it doesn't) OK, thats the condensor taken care of, now lets raise vacuum. Gland steam.....ouch, hot.........2 to 3 psi...........bloody fiddly. Now the air ejectors, opening 150 psi steam to them, gently!, gently! Ahh, good, up she is coming. Excuse me petty Officer, will you pump the oil pump, while I test the trip? Ok, ........OK, and Bang!..that works. Re set it. Pump again please?............ Alright, open the main steam drain............nice whoosh...........shut em, crack the guard valve, crack the throttle...........OK, here she comes, 1000, 2000, 3, 4, .......8000 RPM -hit the trip. Hey, it works!.........reset, and now we open her up to 11000 .............. Down staris, quick, condensor is filling fast, shut the recirc, .......clear of salinity????..........yes, put to system. Open exhaust to the TG, open the guard wide. "Turbo Generator ready to be put on load Petty Officer!!!" "Well done Able , just remember though, Hirate and Okano will want it done a lot quicker than that........and also, remember this is where the Charge watch keeps............so be on your toes!!! Nicely written. We always had a problem with the trip throttle valve on #1 SSTG. No matter how many times it was taken apart and put back together it just never "felt" right, especially once the speed gov. took over and we spun it to engage the trip spring. I took that truk'er apart as a MM2 in 1986 and one final time as a MMC just before transfer in 1990; and multiple times in between. I swear that shaft was about .0015" out of round when you mic'd it vertically, but not when you did it horizontally - which of course makes no sense. It always tripped in PM's just fine, but I also always hoped we never had to rely on it.... Just a feeling. Ya know? Dang that was a while ago. Whipple
< Message edited by Whipple -- 12/9/2012 2:08:47 AM >
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MMCS(SW/AW) 1981-2001 1981 RTC, SD 81-82 NPS, Orlando 82-85 NPTU, Idaho Falls 85-90 USS Truxtun (CGN-35) 90-93 USS George Washington (CVN-73) 93-96 NFAS Orlando 96-01 Navsea-08/Naval Reactors
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